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#1 |
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Location: Gulf Breeze, FL
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Went to the track today hoping for some good results...a mixed bag at best. The good news is I did not break anything and I did not require the use of the winch to load the car hehe.
The car repeatedly shucked out 1.50 60' times and ran 7.26's back to back. The car is leaving like the old Mopar's used to...straight out with barely any front-end upward motion. I believe I am now battling some type of carb issue as it just doesnt hit the tires hard like it once did. Don't believe it has anything to do with the spring or shock changes. The GoPro video shows nothing of real interest that I can pick out. I had another camera pointing at the pinion, but the angle was ineffective rendering the video pretty much useless. From the above video it appears to get some pretty good rotation tho. I'll have to fashion a bracket to get the camera more in front and level with the yoke. With only one lowering block installed the ride height is slightly higher than previous...figured I would let it ride for a bit to see if the new springs settle any. ![]() ![]() Here are the old motor mounts I pulled out of the car. There was almost a 1/2" difference in height between the two...likely the culprit for the cracked cases. ![]() ![]() I will keep at it until I find the bug.
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Rich Taylor I/SA - 321 Last edited by HandOverFist; 05-04-2014 at 11:32 AM. |
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#2 |
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Location: Crookston, MN
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Good luck on getting your car dialed in Rich. I hope your breakage issues are over and it is just fine tuning the combination.
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1969 camaro, pump gas 540"bbc, jerico 1967 camaro, pump gas efi 620", coan t-400 |
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#3 |
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Location: Middletown, IN
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What is your converter flashing to? its either the carb or the converter... didnt you do some 1.45's before?
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1968 Bird/TRW 455/Home ported 13's, '70 Qjet,Holley Street Dominator manifold, Comp Solid FT, 10.817/122.30/1.440 Workin' on E/SA combo ![]() |
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#4 |
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I did not look at the tach yesterday...probably should have. If it turns out to be the convertor I may have to re-think this automatic deal.
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Rich Taylor I/SA - 321 |
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#5 |
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Sounds like it is too tight... you could always try different carb, to see if that is it... My $ is on the converter... didnt look like it spun any...
What brand are you using? The videos from your prior testing, looked pretty good...but you have changed converter since then, correct? Too bad you dont have a 350 turbo in there...probably easier to find a converter to swap in ... Atleast you made it down the track... I dropped heads off today...My new cam should be coming in , early this week...
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1968 Bird/TRW 455/Home ported 13's, '70 Qjet,Holley Street Dominator manifold, Comp Solid FT, 10.817/122.30/1.440 Workin' on E/SA combo ![]() |
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#6 |
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Nope...same ATI convertor.
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Rich Taylor I/SA - 321 |
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#7 |
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put a 1/4'' stroker in it...nobody will ever know...hehe
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1968 Bird/TRW 455/Home ported 13's, '70 Qjet,Holley Street Dominator manifold, Comp Solid FT, 10.817/122.30/1.440 Workin' on E/SA combo ![]() |
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