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#2 |
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Join Date: Oct 2004
Location: Hickory, Ky
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Just spent $1,000 plus on two sets of springs and two sets of main bearings.
I must be crazy. |
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#4 |
Live Reporter
Join Date: Oct 2004
Location: Hickory, Ky
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It was a good decision that I ordered two sets of main bearings because one set was damaged in shipping. The package was mishandled so bad it broke all the air bags that were to cushion the parts in transit. In defense of the seller the parts were direct ship from the manufacturer. Clearance on the mains is good on one and rest need to be adjusted a small amount. Top to bottom I had a good day racing.
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#5 |
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Join Date: Oct 2004
Location: Hickory, Ky
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Getting old always makes you look for the easier pathway. My block has five main caps with 26 fasteners with a three step torque sequence on 16 of them. So I decided to take a shortcut and skip the last step and check clearance. It was in no way predictable and off a mile. I finished the last step and everything was as it should be. I knew better.
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#6 |
Live Reporter
Join Date: Oct 2004
Location: Hickory, Ky
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I am disappointed in making this post.
I've been on hold on customer service for two hours and in that time I have went from 34th in ?Q? to 22 in two hours. Buckeye sales needs to have better customer service and support. Last edited by Larry Hill; 07-22-2024 at 03:19 PM. |
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#7 |
Live Reporter
Join Date: Oct 2004
Location: Hickory, Ky
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In mixing and matching the bearing shells the SOT (Stupid Oldman Trick) bit me in the butt. Old folks should not try to do any work in their head, there is no room, it is full of useless information. Long story short I put the wrong shells in the caps and the clearances were way off. After disassembling I miked the shells and replaced thick ones with thinner ones and everything looks like it might work. We will know on dyno day.
Thanks Mr JR and Mr Byrd |
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