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#1 |
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Join Date: May 2014
Location: Wilmington NC
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Cracked 454 block from water jacket running toward lifter valley. Repairable? If so, would it be worth the expense? It's a 98 from a 3500 HD dually. If it matters, it's an L29 option. I'm under the impression the heads flow very good and would be good to keep. Hopefully the picture shows a good image of the damage.
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William Kilduff 1970 Barracuda (still under construction, indefinitely) 1968 Camaro SS/C |
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#2 | |
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Join Date: Feb 2007
Location: NORTHEAST
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I have always used the Lock-N-Stitch method with real good results. Welding the crack once the weld cools it will just crack again. |
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#3 |
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I have a engine was locked up rod seized to crank in piedmont nc area if interested . 454 out of 98-99 3500
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#4 |
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Jeff Taylor has several 454's in house and my guess you could get a good block, that has been checked, prepped, and ready to go.
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#5 |
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Was this block bored. If so how much over?
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Nelson Kowal Stock 345 |
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#6 |
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Join Date: May 2014
Location: Wilmington NC
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Thanks for the response guys. Been away from the computer for a while working.
This is one I'm debating on having repaired for a future build, if it's worth repairing. If not worth the repair, guess we'll see how much the scrap man says it's worth..LOL. Heads are in great shape, recently back from getting spruced up at machine shop. Had around 140,000 miles on it when we pulled it. As far as I know, it's never been bored, I'm pretty sure it's original to the truck. Ran great, aside from occasional white puff from exhaust. pulled heads to check for blown head gasket and found the crack.
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William Kilduff 1970 Barracuda (still under construction, indefinitely) 1968 Camaro SS/C |
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