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#1 |
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I would be surprised if it's an EFI problem.
What system do you have? Using a data logger?
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Ed Wright 4156 SS/JA |
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#2 |
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I'd check the rubber brake line hose at the rear end housing.I've had 2 that all of a sudden would let fluid through under pressure but internally had collapsed and wouldn't let the pressure release. Same symptoms on our car as yours.Hope you get it fixed fast without a lot of trouble.
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Bill Bogues 4696 STK |
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#3 |
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Compare incrementals and see where you are off.
If your A/F ratio and RPM are the same, odds are your timing is as well. If your RPM is the same, but your MPH is low.................. The humidity is 22% higher on the slower pass. What change did you make with the oil (and filter)?
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Alan Roehrich 212A G/S |
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#4 |
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Incrementals- 60- 1.48-1.53
594-6.75-6.92 660-7.24-7.42 1000-9.55-9.79 1320-11.52-11.82 The 330's were not working either day. Thanks so far guys, J.R. |
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#5 |
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Alan, oil was Mobil 5-30 and stock filter G.M. A.C. Delco before and after,
no changes on either. I try not to introduce any variables unless I'm at the track while I'm sorting out this new to me combo. J.R. Ed, Datalogger is an Accel Gen.7. I am able to download it, but cannot get graphs lately. J.R. |
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#6 |
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Did you measure the amount of oil you drained out? Maybe it is carrying more now,
If it has the same RPM but lost 8 MPH then it about has to be in the converter. |
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#7 |
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I would shy away from any AC Delco filters. I had several collapse due to plastic internals. Cost me an engine. Check the filter it could be collapsed. Now I run a System One reusable filter. No more passenger car filters or oil.
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Mike Pearson 2485 SS |
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#8 |
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^^ That 8 mph difference is what stood out to me.
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Alan Mackin Stock 3777/ SS 3377 P/SA & SS/PA Fox Thunderbird I/PS '95 Mustang GT |
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I've seen where a two-step would intermittently come off and on during a run as the car vibrations made the switch connections. Picked it up on the data logger for the ECU.
Also seen where the O2 sensor has went bad threw the computer into safe mode since when the sensor fails it fails lean. Check TPS and throttle opening 100% physically. Could be a valve hanging open at the top of the rev range or ring flutter also. Lots of possibilities just have to start the process of elimination with any data you have.
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#10 | |
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