|
|
![]() |
#1 |
Member
Join Date: Mar 2003
Location: Mills River, NC
Posts: 417
Likes: 0
Liked 0 Times in 0 Posts
|
![]()
In early 1975 we built a 350 stocker motor for our '69 Nova using the minimum deck height allowed in the NHRA tech bulletin. Put on a pair of RHS prepared cyl. heads using the Chev steel shim gaskets (.017"). Took the car to the Suffolk, VA Div. 2 points meet May 3rd. and set the J/SA record.
Upon tear down for certification we saw that every piston had been hitting the heads. Only way to salvage that motor was to go to thicker head gaskets. Realized then that you didn't want to cut the deck much more than what you needed just to square the block.
__________________
Bobby & Norene Zlatkin L/SA |
![]() |
![]() |
![]() |
#2 |
Junior Member
Join Date: Jul 2006
Posts: 51
Likes: 0
Liked 0 Times in 0 Posts
|
![]()
.032-.034 Clearance and the more you hone it the more you will need.
|
![]() |
![]() |
![]() |
#3 |
VIP Member
Join Date: Oct 2008
Location: Somerset,Ky
Posts: 1,371
Likes: 352
Liked 306 Times in 103 Posts
|
![]()
Around .040 piston/ head clearance is safe for steel rod engine. My 305 dish pure stocker is @.024 with out hitting but I've kept getting closer in small steps I didn't put that close all at once which thats as close
as I'm allowed (with .002 insurance added) I turn 6800 rpm max. If you go under .040 do it carefully if no contact move .005-.010 closer. If have .150 piston-valve either don't have aggressive lobe cam or didn't check correctly.You did check P-V with cam degreed where will be run?You're closest spots were around 10 degrees btdc on ex.and about 10 degrees atdc on int. right?You used solid lifter? I don't know you just trying make sure you're headed right direction and make sure are checking P-V correctly.Have people come in my shop all time that think you check P-V @max lift or tdc.they just don't know any better.On stockers the most I've had from.070 to .090 I've had mine is at .070 int.&ex. for a few years.Below.090 you need to be cautious it's trial and error if they'll touch or not.Int. will live slightly closer than ex. Int. will gain slight clearance ex. will lose slight clearance when running.Load valve train( like its ran springs @all, ready to run)recheck P-V clearance you'll see different clearances.Like M Howard said more piston rocks in bore more clearance you'll need Mike Taylor 3601 Last edited by Mike Taylor 3601; 01-21-2009 at 07:16 PM. |
![]() |
![]() |
![]() |
#4 |
Junior Member
Join Date: Sep 2008
Location: Moore, OK
Posts: 54
Likes: 0
Liked 0 Times in 0 Posts
|
![]()
Well, I guess I should have explained a little better on what I am building. I don't pretend to classify myself as an engine builder, but I have built a few small block racing engines. Since this is my first stocker build...I am trying to get everything that I can get out of this power-wise and knowledge-wise.
I am building a 307...just trying to go a couple tenths under...hopefully. This engine will not turn over 6000rpm to speak of, the piston rock is approximately.005 and on the high end it sits about .002 in the hole. I don't have a very aggressive duration cam and therefore am hopeing that is why I seem to have a decent amount of P-V clearance. I hope that I can get away with about .022 to .025 piston to head clearance to increase my compression as much as possible.
__________________
Tim Wilson HR/SST 4301 |
![]() |
![]() |
![]() |
|
|