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#1 |
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Join Date: Dec 2021
Location: Pukwana SD
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. Bill I tried two on the dyno at Trumble shop both were 5 to 7 hp less than the iron.
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#2 |
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Location: Belmont N.S. Canada
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You want to try an iron intake, the ?crowfoot? version seems to be the one to use
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Chris Chapman 1969 Chevelle NHRA F-G/SA 1090 |
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#3 |
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Welp, looks like the stocker is going to be down for a while. Killed a new to me set of tires and completely sheared off an adjustable 4-link bar. I'm thankful the car stayed rubber side down and that I didn't blow a tire or lose the entire rear-end. Not sure when the bar broke, on the first pass or on the trailer on the way to Wilksboro Dragway. Either way my wagon is down for the count. I'll get it fixed and back going straight again before too long!
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Dawson Pauley #2827 N/SA 1980 Malibu SW 2S 305/180 #2827 S/ST 1978 Mazda RX7 w/ 383 sbc/glide |
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#5 |
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May want to check for Binding throughout the rear suspension travel when you start putting it back together.
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Div 3 Sales, Service and Tech for many manufacturers |
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#7 | |
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When I get back to my shop again I'll snag a pic of the tire off the car, it's paper thin where it wore on the frame rail.
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Dawson Pauley #2827 N/SA 1980 Malibu SW 2S 305/180 #2827 S/ST 1978 Mazda RX7 w/ 383 sbc/glide |
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#8 |
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May i suggest to look at the junction of the axle tube to the center section of your housing. You could find welds broken there which could also explain why your car lift the front driver side higher than the passenger side.
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#9 |
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The plan right now is to replace both 4-link double adjusters on both upper bars and completely re-setup the 4 link to a true neutral setting. That way I can rule out any binding or pos/neg preload that might have been introduced in the car. I will also check the housing, 4-link brackets, and torque-boxes for any warping or damage. Right now I'm on hold with all my cars because my main workhorse (my mazda) needs work desperately and the transmission in my truck welded all of it's forward clutched together. Even if I had a raceable car (0 for 2 right now), I have no way to get either of them to the race track for the next few weeks.
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Dawson Pauley #2827 N/SA 1980 Malibu SW 2S 305/180 #2827 S/ST 1978 Mazda RX7 w/ 383 sbc/glide Last edited by JP1738; 07-15-2024 at 11:02 AM. |
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