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#1 |
Senior Member
Join Date: Dec 2008
Location: Rainy Washington
Posts: 609
Likes: 12
Liked 223 Times in 73 Posts
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So off the sheet like you were never even there?
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#2 |
Member
Join Date: Jun 2007
Posts: 425
Likes: 1
Liked 52 Times in 9 Posts
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One free pass for the freeway . lol
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#3 |
Member
Join Date: Nov 2002
Location: Freeport, IL
Posts: 467
Likes: 660
Liked 232 Times in 39 Posts
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Paul,
What was wrong with the head............cc's, part number, illegal modifications, or????
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Marty Buth 3657 STK |
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#4 |
Member
Join Date: Jun 2007
Posts: 425
Likes: 1
Liked 52 Times in 9 Posts
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cc
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#5 |
Live Reporter
Join Date: Oct 2004
Location: Hickory, Ky
Posts: 10,651
Likes: 1,943
Liked 10,769 Times in 2,238 Posts
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To many or to few?
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#6 |
Member
Join Date: Jul 2006
Location: Phoenix, Arizona
Posts: 133
Likes: 3
Liked 31 Times in 7 Posts
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This was the first real race motor I built for the car. I was running out of time trying to get the motor put together for the race. I did check the valve size, cam lift, bore, stroke, carb, etc, etc. etc. The only thing I didn't check was the cc on the combustion chamber,as I don't have a burret. As it was, I first fired the motor on monday nite after work and left wednesday after work. Seated the rings on the first pass, or maybe the second pass. I had problems with the car all weekend. I finally figured out what the problem was... Carb !!!! gonna need a new one by the way. I decided to go after the record as it is one of the things I always wanted to do when I started racing stock. When the motor was tore down everything checked good, actually better than good, except the CC in the combustion chamber. It was 1.5 cc too small. When I talked to the gentleman that did the heads for me, we found out a two numbers got transposed. It happens, it was an honest oversight. I'm NOT mad at him, I still respect him and have no hard/bad feelings towards him. 1.5 cc isn't gonna make much of a difference on my turbo motor, but the rules are the rules. This is my fault, as I was the one that bolted the heads on the motor and put the motor into the car !! I thanked the Tech Guys Ben and Pat, and told them I was sorry for wasting their time, and would not have gone after the record knowing the issue with the heads. I have always prided myself on being honest, above board, with integrity and morals. I think those that know me would say that I'm not the kind of person to try and cheat or sneak something by and get away with it. I won't even try to use something marginal. Am I disappointed, yes, but more than anything I'm embarrassed that I made myself look like I was trying to cheat. Depending on what NHRA decides to do, I will come back with a motor completely apart, let them check it and assemble it right in front of them, there in the pits if I need to. There are a few things that I still want to accomplish in stock eliminator, if I get to do them, great, if not, it's been an awesome experience, and I want to thank all of you for the fun !! Don't worry Marty, your record is still ok !!!
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#7 |
Member
Join Date: Nov 2002
Location: Freeport, IL
Posts: 467
Likes: 660
Liked 232 Times in 39 Posts
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Rick.............you are a stand up guy for posting this information. I honestly feel bad for you. I knew you felt you were legal or you wouldn't have gone for the record. I wish you all the best.
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Marty Buth 3657 STK |
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#8 |
Member
Join Date: Feb 2002
Location: Phoenix, AZ
Posts: 163
Likes: 32
Liked 22 Times in 7 Posts
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Ive known Rick a long time and can vouch for his honesty and integrity......I feel very bad for the rollercoaster of emotions that he went through yesterday.......ALSO !!!! Congratulations to the Buth clan for setting the O/SA record.....I still hold the performance aspect in high regards
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#9 |
Veteran Member
Join Date: Mar 2005
Location: Sand Springs, OK
Posts: 8,132
Likes: 896
Liked 390 Times in 170 Posts
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I doubt anybody thinks you knowingly built an illegal engine. Nobody would be dumb enough to try to set a record knowing their head was 1.5 cc too small. Stuff happens.
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Ed Wright 4156 SS/JA |
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