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#1 |
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Join Date: Dec 2010
Posts: 299
Likes: 3
Liked 36 Times in 26 Posts
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Curious, does the block and heads have steam holes, do you run a alternator? Just don't trust electric instruments, when strange things are going on.
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#2 |
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Join Date: Dec 2010
Posts: 299
Likes: 3
Liked 36 Times in 26 Posts
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And where is the temp sensor located?
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#3 | |
Member
Join Date: Mar 2016
Location: Crete, IL
Posts: 167
Likes: 265
Liked 54 Times in 24 Posts
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The sensor was in the left front corner of the intake manifold. For a test we moved it to the left rear corner of the intake. It does not have a coolant cross over in the rear, but was in the coolant passage. No difference in the data log. Yes on the alternator. |
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#4 |
VIP Member
Join Date: Oct 2008
Location: Somerset,Ky
Posts: 1,380
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Liked 317 Times in 108 Posts
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Don't want to insult anyone with a question like this,but haven't seen it mentioned, the head gaskets are marked front and they are on correct?? doesn't have belt driven water pump of some sort rotating wrong direction?
Just mentioning some basics hadn't seen mentioned. electric style gauge readings can be screwy sometimes,have seen sealer on threads of sensor cause bad ground for sending unit and read incorrect or not at all. Mike Taylor 3601 |
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#5 | |
Member
Join Date: Mar 2016
Location: Crete, IL
Posts: 167
Likes: 265
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The gaskets are on correctly. No insult taken. The water pump is a Pro-Form Electric. The owner is going to try swapping a Meziere pump off his other car, as well as removing a medium size restricer from the T-State housing and test. As for the sensor, we are referring to a 3 wire sensor for the Holley EFI data log. We have tried another sensor with same result to rule that out. Also have found out that the car had a puke tank for the Radiator and he changed that out to a recovery tank. Once I hear results of testing after these changes I will update post. Thanks- T Gross |
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#6 |
Member
Join Date: Mar 2016
Location: Crete, IL
Posts: 167
Likes: 265
Liked 54 Times in 24 Posts
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Update*
Customer tested last night. No problems. Monitored during multiple runs. Although 3 things were changed, I believe the addition of the recovery tank was the helper here. It appears that the Siamese cylinders of the Dart block is not as forgiving when it comes to moving air pockets that were introduced after cool off. |
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